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  1. 8

    “Pre alpha” leak

    The drive was recently off the boat. Replaced the whole impeller housing including the base plate. Also did the shift shaft bushing. Didn’t go any further than that or even look at the condition of the carrier. When the carrier leak happened I noticed the outer prop shaft seal looked like it...
  2. 8

    “Pre alpha” leak

    Oh, I was talking about Mercruiser. From what I gathered online the consensus was don’t go over 15psi. I just landed on 11 pounds mainly cause I was scared to go higher, it held for 2 hours. I washed everything and blew it out with compressed air so it was clean and bone dry. Sat full of gear...
  3. 8

    “Pre alpha” leak

    Copy that. From what I’ve gathered 15 psi is the max. I’m coming up on 1.5 hours and still holding 11psi. Perhaps it was residual oil from assembly. I’m gonna let it ride and see what happens. I’ll post back. As always, thank you!
  4. 8

    “Pre alpha” leak

    Just to clarify, it went from leaking to just a few drops AFTER using the permatex, there’s no trails of oil leaking from anywhere else. So I think I almost got this thing. None of this seep has been under pressure. Just static leakage from its own weight. I drained the gear lube for the...
  5. 8

    “Pre alpha” leak

    I just got home and still have a very tiny leak.. Son of a b!$@& Looking at the back side of the carrier you can see a good bead of the permatex aviation sealant all the way around it. The leak is coming from the 6 o’clock position. Very tiny amount of oil, I know it’s not residual because I...
  6. 8

    “Pre alpha” leak

    Yea, i hear ya! To be honest i was just kinda nervous to use it on the drive. Obviously something told me to use it as a little extra insurance but I was very conservative with it. Then per your recommendation, this time around I used a heavier amount. I hope this thing holds, I’m getting tired...
  7. 8

    “Pre alpha” leak

    After cleaning the bore with scotch brite, a brass brush, 0000 steel wool and cleaning up with acetone and compressed air (gears protected of course) I think I got it sealed. Had to use more permatex this time around. Just a heavier coat. Not runny or globbed on just a thicker, heavier...
  8. 8

    “Pre alpha” leak

    I’m thinking I’ll put my money on both this time around!
  9. 8

    “Pre alpha” leak

    Well, the surface could definitely be cleaner. I’ll pull her back apart and take a better look. I just hit it with scotch brite the picture is what it looked like before cleaning. And good to know I can be a little more aggressive with the sealant if need be. The weird thing is, how the hell...
  10. 8

    “Pre alpha” leak

    It’s for sure coming from behind the carrier.. I think ghost is onto something..
  11. 8

    “Pre alpha” leak

    1975 pre alpha drive randomly started leaking gear lube from the bearing carrier at the prop shaft. The leak appears to be coming out past the main large o ring on the carrier. Pulled carrier, found a very old and very tired O ring. Replaced that and both oil seals. Held oil for about 24 hours...
  12. 8

    75 Formula Shift Issue

    I did have the coil wire on the wrong side initially, when I got continuity on the meter I noticed and switch it to the other side of the block that is isolated and it was still grounding out somehow. Regardless, the problem has been solved and I’m feeling confident about it. Is what has me...
  13. 8

    75 Formula Shift Issue

    UPDATE*** Today I jumped back in the boat on the trailer, Four things were discovered.. One, the interrupter switch was never even wired to the coil negative. 51 years is a lot of time for someone to do some backdoor wiring for some reason (not even sure if that’s possible) but remember, it...
  14. 8

    75 Formula Shift Issue

    Heres a before and during shift screen shot from a video I took during a forward shift. I ordered a “new switch” and am going to verify wiring as soon as the boats back at the house where I can look into it. Again, the boat shifts fine. It’s coming out of gear that’s the problem so everything...
  15. 8

    75 Formula Shift Issue

    I used a led pod light (all I had) wired from a 12v battery through the switch. Closing the switch kills the light, with the switch open the light comes back on. With the switch closed (arm depressed) the light will flicker if I tap the switch. I think I need to verify down stream electrical...
  16. 8

    75 Formula Shift Issue

    I agree with you but I still think there’s something up with the switch itself. Still worth investigating for sure. But, if wiring was the issue, I feel like the problem would be more intermittent outside of something coming completely disconnected. Which I know isn’t the case because I have...
  17. 8

    75 Formula Shift Issue

    UPDATE*** Launched the boat today, same issue, played around with it a bit to no avail. Notched shift plate working as it should depressing switch arm. I had already verified continuity from the switch to the coil, with the engine running I manually closed the switch and nothing happened. When...
  18. 8

    75 Formula Shift Issue

    I hear ya. Dipping the boat tomorrow morning, I still find the whole thing weird. This isn’t my first rodeo and that boat was shifting in and out of gear smooth as butter one weekend, and not so much the other. Shift adjustment procedure definitely required more adjustment than I would have...
  19. 8

    75 Formula Shift Issue

    how much adjustment is considered normal or within the realm of “normal” off that 7/16 stud? It was about half way center of the slot. I moved it all the way towards port checked gears and called it a day. Was thinking last night maybe that was supposed to be a little more of a fine tuning...
  20. 8

    75 Formula Shift Issue

    I followed your instructions exactly, was surprised how much adjustment was needed. Nothing crazy, but definitely needed it. I’m thinking the issue may have been at the upper shift cable. It’s original to the boat as far as I know so I’m sure it’s a bit tired to say the least. Reverse didn’t...
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